The Drive Train
The Belt Drive
Our drivetrain is a relatively simple set of timing belt drives, one for each of the rear wheels to generate the desired rear-wheel drive. The pulleys were ordered from McMaster-Carr here (https://www.mcmaster.com/timing-belt-pulleys), and the belt itself was also from McMaster-Carr, linked here (https://www.mcmaster.com/belts). The pulleys used were the XL Series Lightweight Timing Belt Pulleys with an OD of 1” and 2”, to create a 2:1 gear ratio in our drivetrain. The timing belt was the XL Series Timing Belt, with a width of ¼” and an outer circle length of 15”, to give us about five inches between the center of each pulley.
Implementation
The ordered pulleys worked great, but we needed to get the larger pulley to fit around the truck structure - it was either this or somehow modify the fairly expensive trucks, so we opted to modify the pulleys. The pulley consisted of a central metal core to fit the shaft of whatever is holding the pulley, and a plastic outer piece with the timing belt teeth. We used an arbor press to try and remove the press-fit metal core, but only broke the pulley.
Disappointed but not discouraged, we came up with a new solution - try and freeze the pulley, as metal shrinks when it is cold. With permission from the bio/chem labs at our school, we placed the pulley in the -80 degrees Celsius freezer (-112 deg Fahrenheit) for about 24 hours. Hopeful, we removed the pulley, put it in a cold bag with ice, and transported it to the arbor press in the machine shop. Once again, the we had no luck - the pulley snapped, though it was cleaner than the last break.
Out of time and money, we decided to try 3D printing our own pulleys by utilizing the CAD McMaster-Carr provides. Using the same files, but removing a 1.25” circle from the center of the pulley, it proved to be a success. The pulleys worked and even matched our board’s color scheme.
In an attempt to increase the surface area between the wheels and the pulleys, we designed a pulley with a dome to match the curvature of the inside of the wheels. We also increased our larger pulley outer diameter for the final print to be 2.53”, to once again increase our gear ratio and get more torque out of our motors.